bdring / FluidNC

The next generation of motion control firmware
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Problem: Withdrawn: After updating FluidNC firmware to 3.7.18, old WebUI version shown (not v3) #1243

Closed DougJoseph closed 5 months ago

DougJoseph commented 5 months ago

Wiki Search Terms

WebUI

Controller Board

Jackpot by V1 Engineering (based on 6-pack)

Machine Description

LowRider v3

Input Circuits

No response

Configuration file

board: Jackpot TMC2209
name: LowRider
meta: 10-30-2023 RyanZ; 11-20-2023 DougJoseph for swapped X and Y

planner_blocks: 32

stepping:
  engine: I2S_STATIC
  idle_ms: 255
  pulse_us: 4
  dir_delay_us: 1
  disable_delay_us: 0

uart1:
  txd_pin: gpio.0
  rxd_pin: gpio.4
  rts_pin: NO_PIN
  baud: 115200
  mode: 8N1

uart2:
  txd_pin: gpio.14
  rxd_pin: gpio.13
  rts_pin: NO_PIN
  cts_pin: NO_PIN
  baud: 1000000
  mode: 8N1

uart_channel2:
  uart_num: 2
  report_interval_ms: 75

axes:
  shared_stepper_disable_pin: NO_PIN

  x:
    steps_per_mm: 50.000
    max_rate_mm_per_min: 9000.000
    acceleration_mm_per_sec2: 200.000
    max_travel_mm: 2495
    soft_limits: true
    homing:
      cycle: 3
      positive_direction: false
      mpos_mm: 0
      feed_mm_per_min: 300.000
      seek_mm_per_min: 1500.000
      settle_ms: 500
      seek_scaler: 1.100
      feed_scaler: 1.100
    #X
    motor0:
      limit_neg_pin: gpio.33:high
      limit_pos_pin: NO_PIN
      limit_all_pin: NO_PIN
      hard_limits: true
      pulloff_mm: 4.000
      tmc_2209:
        uart_num: 1
        addr: 1
        cs_pin: NO_PIN
        r_sense_ohms: 0.110
        run_amps: 0.680
        hold_amps: 0.500
        microsteps: 8
        stallguard: 0
        stallguard_debug: false
        toff_disable: 0
        toff_stealthchop: 5
        toff_coolstep: 3
        run_mode: StealthChop
        homing_mode: StealthChop
        use_enable: false
        step_pin: I2SO.5
        direction_pin: I2SO.4
        disable_pin: I2SO.7

    #A
    motor1:
      limit_neg_pin: gpio.35:high
      limit_pos_pin: NO_PIN
      limit_all_pin: NO_PIN
      hard_limits: true
      pulloff_mm: 4.000
      tmc_2209:
        uart_num: 1
        addr: 3
        cs_pin: i2so.14
        r_sense_ohms: 0.110
        run_amps: 0.680
        hold_amps: 0.500
        microsteps: 8
        stallguard: 0
        stallguard_debug: false
        toff_disable: 0
        toff_stealthchop: 5
        toff_coolstep: 3
        run_mode: StealthChop
        homing_mode: StealthChop
        use_enable: false
        step_pin: I2SO.13
        direction_pin: I2SO.12
        disable_pin: I2SO.15        

  y:
    steps_per_mm: 50.000
    max_rate_mm_per_min: 9000.000
    acceleration_mm_per_sec2: 200.000
    max_travel_mm: 1250
    soft_limits: true
    homing:
      cycle: 3
      positive_direction: false
      mpos_mm: 0
      feed_mm_per_min: 300.000
      seek_mm_per_min: 1500.000
      settle_ms: 500
      seek_scaler: 1.100
      feed_scaler: 1.100
    #Y
    motor0:
      limit_neg_pin: gpio.25:high
      limit_pos_pin: NO_PIN
      limit_all_pin: NO_PIN
      hard_limits: true
      pulloff_mm: 4.000
      tmc_2209:
        uart_num: 1
        addr: 0
        cs_pin: NO_PIN
        r_sense_ohms: 0.110
        run_amps: 0.680
        hold_amps: 0.500
        microsteps: 8
        stallguard: 0
        stallguard_debug: false
        toff_disable: 0
        toff_stealthchop: 5
        toff_coolstep: 3
        run_mode: StealthChop
        homing_mode: StealthChop
        use_enable: false
        direction_pin: I2SO.1
        step_pin: I2SO.2
        disable_pin: I2SO.0

  z:
    steps_per_mm: 200.000
    max_rate_mm_per_min: 1200.000
    acceleration_mm_per_sec2: 80.000
    max_travel_mm: 125.000
    soft_limits: true
    homing:
      cycle: 1
      positive_direction: true
      mpos_mm: 0
      feed_mm_per_min: 300.000
      seek_mm_per_min: 800.000
      settle_ms: 500
      seek_scaler: 1.100
      feed_scaler: 1.100

    motor0:
      limit_neg_pin: NO_PIN
      limit_pos_pin: gpio.32:high
      limit_all_pin: NO_PIN
      hard_limits: true
      pulloff_mm: 4.000
      tmc_2209:
        uart_num: 1
        addr: 2
        cs_pin: NO_PIN
        r_sense_ohms: 0.110
        run_amps: 0.680
        hold_amps: 0.500
        microsteps: 8
        stallguard: 0
        stallguard_debug: false
        toff_disable: 0
        toff_stealthchop: 5
        toff_coolstep: 3
        run_mode: StealthChop
        homing_mode: StealthChop
        use_enable: false
        step_pin: I2SO.10
        direction_pin: I2SO.9
        disable_pin: I2SO.8

     #B
    motor1:
      limit_neg_pin: NO_PIN
      limit_pos_pin: gpio.34:high
      limit_all_pin: NO_PIN
      hard_limits: true
      pulloff_mm: 3.270
      tmc_2209:
        uart_num: 1
        addr: 3
        cs_pin: i2so.19
        r_sense_ohms: 0.110
        run_amps: 0.680
        hold_amps: 0.500
        microsteps: 8
        stallguard: 0
        stallguard_debug: false
        toff_disable: 0
        toff_stealthchop: 5
        toff_coolstep: 3
        run_mode: StealthChop
        homing_mode: StealthChop
        use_enable: false
        step_pin: I2SO.18
        direction_pin: I2SO.17
        disable_pin: I2SO.16

#  c:
#    steps_per_mm: 80.000
#    max_rate_mm_per_min: 5000.000
#    acceleration_mm_per_sec2: 100.000
#    max_travel_mm: 300.000
#    soft_limits: false
#    homing:
#      cycle: 0
#      positive_direction: true
#      mpos_mm: 150.000
#      feed_mm_per_min: 100.000
#      seek_mm_per_min: 800.000
#      settle_ms: 500
#      seek_scaler: 1.100
#      feed_scaler: 1.100
#
#    motor0:
#      limit_neg_pin: gpio.39:low
#      limit_pos_pin: NO_PIN
#      limit_all_pin: NO_PIN
#      hard_limits: true
#      pulloff_mm: 3.000
#      tmc_2209:
#        uart_num: 1
#        addr: 3
#        cs_pin: i2so.22
#        r_sense_ohms: 0.110
#        run_amps: .1
#        hold_amps: 0.050
#        microsteps: 16
#        stallguard: 0
#        stallguard_debug: false
#        toff_disable: 0
#        toff_stealthchop: 5
#        toff_coolstep: 3
#        run_mode: StealthChop
#        homing_mode: StealthChop
#        use_enable: false
#        step_pin: I2SO.21
#        direction_pin: I2SO.20
#        disable_pin: I2SO.23

i2so:
  bck_pin: gpio.22
  data_pin: gpio.21
  ws_pin: gpio.17

spi:
  miso_pin: gpio.19
  mosi_pin: gpio.23
  sck_pin: gpio.18

sdcard:
  cs_pin: gpio.5
  card_detect_pin: NO_PIN
  frequency_hz: 20000000

probe:
  pin: gpio.36:low
  toolsetter_pin: NO_PIN
  check_mode_start: true

start:
  must_home: false

coolant:
  flood_pin: gpio.2
  mist_pin: gpio.16
  delay_ms: 0

control:
  safety_door_pin: NO_PIN
  reset_pin: NO_PIN
  feed_hold_pin: NO_PIN
  cycle_start_pin: NO_PIN
  macro0_pin: NO_PIN
  macro1_pin: NO_PIN
  macro2_pin: NO_PIN
  macro3_pin: NO_PIN  

macros:
  startup_line0:
  startup_line1:
  macro0:
  macro1:
  macro2:
  macro3:

user_outputs:
  analog0_pin: NO_PIN
  analog1_pin: NO_PIN
  analog2_pin: NO_PIN
  analog3_pin: NO_PIN
  analog0_hz: 5000
  analog1_hz: 5000
  analog2_hz: 5000
  analog3_hz: 5000
  digital0_pin: gpio.26
  digital1_pin: gpio.27
  digital2_pin: NO_PIN
  digital3_pin: NO_PIN

#Laser:
#  pwm_hz: 5000
#  output_pin: gpio.27
#  enable_pin: NO_PIN
#  disable_with_s0: false
#  s0_with_disable: true
#  tool_num: 0
#  speed_map: 0=0.000% 255=100.000%
#  off_on_alarm: true

# pwm:
#  pwm_hz: 5000
#  direction_pin: gpio.26
#  output_pin: gpio.27
#  enable_pin: NO_PIN
#  disable_with_s0: false
#  s0_with_disable: true
#  spinup_ms: 0
#  spindown_ms: 0
#  tool_num: 0
#  speed_map: 0=0.000% 1000=100.000%
#  off_on_alarm: false

# 5V out gpio.26/27
# VMot out gpoi.2/16
# In's left to right gpoi.25/33/32/35/34/39/36

Startup Messages

$ss
[MSG:INFO: FluidNC v3.7.18 https://github.com/bdring/FluidNC]
[MSG:INFO: Compiled with ESP32 SDK:v4.4.7-dirty]
[MSG:INFO: Local filesystem type is littlefs]
[MSG:INFO: Configuration file:config.yaml]
[MSG:INFO: Machine LowRider]
[MSG:INFO: Board Jackpot TMC2209]
[MSG:INFO: UART1 Tx:gpio.0 Rx:gpio.4 RTS:NO_PIN Baud:115200]
[MSG:INFO: UART2 Tx:gpio.14 Rx:gpio.13 RTS:NO_PIN Baud:1000000]
[MSG:INFO: uart_channel2 created at report interval: 75]
[MSG:INFO: I2SO BCK:gpio.22 WS:gpio.17 DATA:gpio.21]
[MSG:INFO: SPI SCK:gpio.18 MOSI:gpio.23 MISO:gpio.19]
[MSG:INFO: SD Card cs_pin:gpio.5 detect:NO_PIN freq:20000000]
[MSG:INFO: Stepping:I2S_static Pulse:4us Dsbl Delay:0us Dir Delay:1us Idle Delay:255ms]
[MSG:INFO: User Digital Output:0 on Pin:gpio.26]
[MSG:INFO: User Digital Output:1 on Pin:gpio.27]
[MSG:INFO: Axis count 3]
[MSG:INFO: Axis X (0.000,2495.000)]
[MSG:INFO:   Motor0]
[MSG:INFO:     tmc_2209 UART1 Addr:1 CS:NO_PIN Step:I2SO.5 Dir:I2SO.4 Disable:I2SO.7 R:0.110]
[MSG:INFO:  X Neg Limit gpio.33]
[MSG:INFO:   Motor1]
[MSG:INFO:     tmc_2209 UART1 Addr:3 CS:I2SO.14 Step:I2SO.13 Dir:I2SO.12 Disable:I2SO.15 R:0.110]
[MSG:INFO:  X2 Neg Limit gpio.35]
[MSG:INFO: Axis Y (0.000,1250.000)]
[MSG:INFO:   Motor0]
[MSG:INFO:     tmc_2209 UART1 Addr:0 CS:NO_PIN Step:I2SO.2 Dir:I2SO.1 Disable:I2SO.0 R:0.110]
[MSG:INFO:  Y Neg Limit gpio.25]
[MSG:INFO: Axis Z (-125.000,0.000)]
[MSG:INFO:   Motor0]
[MSG:INFO:     tmc_2209 UART1 Addr:2 CS:NO_PIN Step:I2SO.10 Dir:I2SO.9 Disable:I2SO.8 R:0.110]
[MSG:INFO:  Z Pos Limit gpio.32]
[MSG:INFO:   Motor1]
[MSG:INFO:     tmc_2209 UART1 Addr:3 CS:I2SO.19 Step:I2SO.18 Dir:I2SO.17 Disable:I2SO.16 R:0.110]
[MSG:INFO:  Z2 Pos Limit gpio.34]
[MSG:INFO: X Axis driver test passed]
[MSG:INFO: X2 Axis driver test passed]
[MSG:INFO: Y Axis driver test passed]
[MSG:INFO: Z Axis driver test passed]
[MSG:INFO: Z2 Axis driver test passed]
[MSG:INFO: Kinematic system: Cartesian]
[MSG:INFO: Using spindle NoSpindle]
[MSG:INFO: Flood coolant gpio.2]
[MSG:INFO: Mist coolant gpio.16]
[MSG:INFO: Probe gpio.36:low]
[MSG:INFO: Connecting to STA SSID:The-DR-is-IN_2.4GHz]
[MSG:INFO: Connecting.]
[MSG:INFO: Connecting..]
[MSG:INFO: Connected - IP is 192.168.1.32]
[MSG:INFO: WiFi on]
[MSG:INFO: Start mDNS with hostname:http://fluidnc.local/]
[MSG:INFO: SSDP Started]
[MSG:INFO: HTTP started on port 80]
[MSG:INFO: Telnet started on port 23]
ok

User Interface Software

WebUI

What happened?

After updating the FluidNC firmware to 3.7.18, it is showing me the old version of WebUI. I uploaded the index.html.gz that came with v3.7.18 (which was 117 KB), but still the old WebUI, not v3. Then I overwrote it with the WebUIv3 version of index.html.gz that I was using before (which was 111 KB), but it still shows me the old version of WebUI. I must be overlooking something, but I don’t know what. Any ideas?

GCode File

No response

Other Information

No response

DougJoseph commented 5 months ago

Please consider this as withdrawn.

DougJoseph commented 5 months ago

I gather that webUI related issues are not really something to post here.