So I've got this working with the latest klipper. Runs well.
However I've noticed my X axis is always 2 steps out. Y is perfect everytime. It doesn't matter how high or low I set my acceleration or speed it's always within 1-2 steps out on the second pass.
I'm using Sensorless Homing with tmc2209 drivers on an octopus pro v1.1 board.
Worked out to be my old x and y end mechanical endstops causing the carriage to stop at different points. Removed the physical endstops on the printer and now working as should
So I've got this working with the latest klipper. Runs well.
However I've noticed my X axis is always 2 steps out. Y is perfect everytime. It doesn't matter how high or low I set my acceleration or speed it's always within 1-2 steps out on the second pass.
I'm using Sensorless Homing with tmc2209 drivers on an octopus pro v1.1 board.