The drone drifts right out of the box even after calibration attempts. The gyro movement doesn't reflect in the configurator. And now after trying to offset the right roll on the controller to compensate, the bindings have all gone awry. It was a mode 2 (left joystick throttle) which now has throttle on the right stick, pitch on right stick roll axis, and roll or yaw don't exist anymore. Is there anyway to reverse this action by flashing OG firmware? Have tried all setting and factory reset in Configurator with no results.
The drone drifts right out of the box even after calibration attempts. The gyro movement doesn't reflect in the configurator. And now after trying to offset the right roll on the controller to compensate, the bindings have all gone awry. It was a mode 2 (left joystick throttle) which now has throttle on the right stick, pitch on right stick roll axis, and roll or yaw don't exist anymore. Is there anyway to reverse this action by flashing OG firmware? Have tried all setting and factory reset in Configurator with no results.