Open GoogleCodeExporter opened 8 years ago
I forgot to add that I am using the Hobbyking Multiwii pro FC with MTK GPS. The
motors on my quad are 950kv 2836 with 10x47 props. ESCs are 25A turnigy plush
with a 4500mah 3S battery on a hobbyking Heavy Aerial Lift (H.A.L) quad frame.
The quad flies perfectly in stabilize mode, and in still air it will just sit
in position without drift.
Hit the ALT HOLD and it thinks it's a rocket heading for the moon!
Original comment by arthurwo...@gmail.com
on 25 Mar 2013 at 4:32
Did you moved your throttle at the centre position after switching to ALT HOLD?
Original comment by alberto....@gmail.com
on 27 Mar 2013 at 7:08
Yes, definitely. It was in a steady hover at half throttle before I switched to
ALT HOLD. I've reverted to 2.8R3 and tuned my PIDs and I now get acceptable ALT
HOLD so I think it is a problem with 2.9 r300 version.
Original comment by arthurwo...@gmail.com
on 27 Mar 2013 at 10:19
I have had similar weirdness with the ALT hold in r300.
It seems to climb for me (slowly), but indefinitely. And I don't move my stick
once I have entered ALT hold flight mode.
It worked fine on 2.8 and 2.9's earlier versions. Since changing to r300 I also
had to drop my throttle rate D by 1/2 to get it to stop oscilating in ALT hold
despite not changing anything on my quad. I agree that it seems to over react
the motors.
Original comment by glenwimb...@gmail.com
on 28 Mar 2013 at 12:42
In r289 on that mwc pro board I hawe same issue it keeps climbing the only
difference is how fast from tuning settings up and down. Probably something to
do with it not being those fancy mpu6050 accelrometers that the original code
are built for.
Lointer dont work either keeps climbing Position mode works fine (manual
throttle there)
Original comment by EmilKar...@gmail.com
on 2 Apr 2013 at 6:42
Please, provide more info about your boards (especially which sensors used,
ITG.. MPU...)
Also, do you have sonar and did you enabled it in Mission Planner? Enabled
sonar but not connected, can cause error in Alt_hold.
Original comment by Alexey.K...@gmail.com
on 3 Apr 2013 at 8:41
I'm using CRIUS AIO V1, MPGN2.9r300, sonar disabled and ALT_HOLD works
perfectly if I keep my throttle in the middle position.
Original comment by alberto....@gmail.com
on 3 Apr 2013 at 9:06
I am using the multiwii Pro w/ MTK GPS from hobbyking. I don't have sonar. The
specs are:
• SMD component design with Atmega2560
• ITG3205 Triple Axis Gyro
• BMA180 Accelerometer
• BMP085 Barometer
• HMC5883L Magnetometer
• Servo output for camera pitch and roll control
• Supports direct connection of GPS module (MTK 3329 GPS module included)
• On-board USB connection for programming
Original comment by arthurwo...@gmail.com
on 3 Apr 2013 at 11:22
Same board
I am using the multiwii Pro w/ MTK GPS from hobbyking. I don't have sonar. The
specs are:
• SMD component design with Atmega2560
• ITG3205 Triple Axis Gyro
• BMA180 Accelerometer
• BMP085 Barometer
• HMC5883L Magnetometer
• Servo output for camera pitch and roll control
• Supports direct connection of GPS module (MTK 3329 GPS module included)
• On-board USB connection for programming
My thougts is because i tried tuning like crazy it only changes the speed it
climbes. Is there is some kind of assumptions in the 2.9 code regarding the
original apm2.5 set of sensors.
Original comment by EmilKar...@gmail.com
on 3 Apr 2013 at 4:51
But i will go outside now try an experiment. rasing my throttle from 40% where
it howers to center. I Think i did it yestoday but i wil lmake an extra try to
be shure.
Original comment by EmilKar...@gmail.com
on 3 Apr 2013 at 4:53
So looks like problem with HK Multiwii board with ITG3205 and BMA180, Ok will
try to find problem.
Original comment by Alexey.K...@gmail.com
on 3 Apr 2013 at 5:19
Ok I tested the trottle stick is completly unresponsive can go from center to
100% to 10% without anny difference whatsoever it just climbes at the same
speed.
And now i crashed my quad from a prop coming lose in the air or something like
that. It just vent straight down in stab mode. So will need to rebuild it
before I do some more testing.
Original comment by EmilKar...@gmail.com
on 3 Apr 2013 at 5:23
Thank you Alexey, you are doing a great job! I am really enjoying flying my
quad on 2.8r3, currently experimenting with the auto mode :-)
Original comment by arthurwo...@gmail.com
on 3 Apr 2013 at 8:16
Here is a short link to a video showing 2.8r3 running on the same quad where
loiter and alt hold are working perfectly, very happy with the performance of
the FC on this release.
http://www.youtube.com/watch?v=I9bg919FkAE
Original comment by arthurwo...@gmail.com
on 5 Apr 2013 at 9:46
I am Using the Multiwii Se board as an IMU for my mega and running the 2.9 R5
code the Altitude function makes my copter rise heavily.....
Original comment by prathees...@gmail.com
on 11 May 2013 at 5:33
I am using Multiwii Pro from HK (ITG3205 Triple Axis Gyro, BMA180
Accelerometer, BMP085 Barometer, HMC5883L Magnetometer), no sonar and R300
version.
For me most of the time (6/10) the quad climbs like a rocket with Alt Hold, but
sometimes (3/10) it drops like a rock and eventually (1/10) it keeps the
altitude after some small bumps.
Original comment by ginodoug...@gmail.com
on 20 Aug 2013 at 1:21
Same board and same problem here. Using HK Multiwii Pro with GPS and 2.9 r300
version.
Last night went to test it. Everything was perfect in Stable Mode, but when
changed to ALT HOLD (throttle lower than half) my quadcopter started climbing
really fast, and crashed in a tree branch :(
It climbed so fast that I could'nt do anything to avoid the crash.
Heading back to 2.8 now...
Original comment by mattogo...@gmail.com
on 2 Oct 2013 at 10:44
I have the same problem with an RcTimer Crius AIOP V2 board.
I was using 2.8 R3 and both Loiter and Alt Hold worked great.
I only switched to 2.9 R300 because I was burning out servos with the 490hz
update rate.
Now, when I hover at 1/2 throttle in Stabalize mode and switch to either Alt
Hold or Loiter, it steadily climbs, as others have said. Using stock PID
settings, BTW.
Art
Original comment by ArtSpazi...@gmail.com
on 2 Oct 2013 at 12:00
[deleted comment]
I have the same problem with HK Multiwii Pro with GPS and 2.9 r6 version...
with version 2.8 r3 never had any problem with the halt hold..
the problem occurs after about 2 seconds you have activated the halt old .
even if the stock of the gas is 20% 40% etc....
Original comment by sangrego...@gmail.com
on 2 Oct 2013 at 10:29
no updates with this ????
Original comment by LGallagh...@gmail.com
on 23 Jul 2014 at 10:17
Original issue reported on code.google.com by
arthurwo...@gmail.com
on 25 Mar 2013 at 4:27