Closed GoogleCodeExporter closed 8 years ago
It seems that, somebody has the same problem
http://diydrones.ning.com/forum/topics/channel-6-twitch?xg_source=activity
Original comment by airma...@gmail.com
on 16 Mar 2012 at 2:19
[deleted comment]
I noticed the same problem, but twitching appears around 1/2 throtle stick position (testet on the ground without ESCs). I wonder if it could be some channel interference and encoder problem ?
Original comment by dj_...@wp.pl
on 13 Apr 2012 at 10:17
DJ,
If you're using an APM1 and have an atmel programmer, could you try upgrading the ppm firmware according to the instructions on this wiki page? I can't guarantee a solution but it seems to be helping some people.
http://code.google.com/p/arducopter/wiki/Encoder
Original comment by rmackay...@gmail.com
on 16 Apr 2012 at 12:38
I can't say I've noticed this any more on APM2, 2.5.5.
Thanks all.
Original comment by crispin....@gmail.com
on 31 May 2012 at 7:27
I am also having problems with gimbal setup, The ch10. is twitching but
working, The ch11 is twitching (more than ch10) and is working.
I have connected the servos to Ch 10 and Ch11, enabled tilt and roll servo in
mission planner.
Running the V2.7.1 Hexa Firmware.
Tested with New Futaba S3156 Digital servos
Tested with New JR ES539 Analog servos
Results is consistent with all tested servos.
I am looking for a solution to the problems but have not been able to figure it
out.
Helge.
Original comment by Laptop2...@hotmail.com
on 20 Aug 2012 at 6:44
Running MegaPirateNG 2.9r5 and the same problems exist on ch10&11 assigned to
gimbal. Seems fine on the ground but once in flight the jitters start close to
end of 4 minute flights. Tried 5&6 and the jitter was insane.
With MP 2.7r4 using channels 7&8 all was good. I realize that MP for the Crius
is a port but the problems seem identical.
Cheers,
Andy
Original comment by andyho...@gmail.com
on 13 Feb 2013 at 5:24
I hawe twitches on my gimbal to on megapirateng 2.9 on both pitch and roll.
it works perfekt but it get twitches about avery 3 sek I think there is some
problem with the signal not updating smothly enough. Conected to a reciver
these hitec digital servos I use are perfect smooth and flawless. Had same
problem with cheap servos to but way way worse.
Original comment by EmilKar...@gmail.com
on 30 Mar 2013 at 7:06
I have the same twitch. Is there anyone working the problem? Or know of the
solution?
Original comment by sto...@gmail.com
on 29 Jun 2013 at 11:12
Closing all issues on the old issues list by marking them WontFix.
If this is still a valid issue please re-raise it on the new GitHub issues
list: https://github.com/diydrones/ardupilot/issues
Thanks!
Original comment by rmackay...@gmail.com
on 21 Jul 2013 at 2:14
Original issue reported on code.google.com by
airma...@gmail.com
on 12 Mar 2012 at 7:32