Spark-Concepts / xPro-V5

xPro-V5 CNC Motion Control System Documentation and User Information
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Steppers not moving #216

Open Druidroid opened 1 year ago

Druidroid commented 1 year ago

I got fluent update and uploaded yaml file with the correct settings, and yet the machine doesnt move at all. When i connect via COM4 @ 115200 baud steppers make a sound but then i just cant jog on any axis and steppers doesnt react in any way, problem persist since when i had the previous firmware but back then the motors reacted by making a sound and now with fluent doesnt even make a sound.

What can be the problem? Its an Ultimate Bee from Bulkman with high torque steppers. Below I put what i get on the Gcode sender.

Connected to COM4 @ 115200 baud ets Jun 8 2016 00:22:57 rst:0x1 (POWERON_RESET),boot:0x17 (SPI_FAST_FLASH_BOOT) configsip: 0, SPIWP:0xee clk_drv:0x00,q_drv:0x00,d_drv:0x00,cs0_drv:0x00,hd_drv:0x00,wp_drv:0x00 mode:DIO, clock div:1 load:0x3fff0030,len:1184 load:0x40078000,len:13220 ho 0 tail 12 room 4 load:0x40080400,len:3028 entry 0x400805e4 E (601) esp_core_dump_flash: No˜¬K•�dump partition found! E (601) esp_core_dump_flash: No core dump partition found! [MSG:INFO: FluidNC v3.7.0] [MSG:INFO: Compiled with ESP32 SDK:v4.4.4] [MSG:INFO: Local filesystem type is littlefs] [MSG:INFO: Configuration file:config.yaml] [MSG:INFO: Machine xPro V5 Ondrej ] [MSG:INFO: Board XPro V5] [MSG:INFO: SPI SCK:gpio.18 MOSI:gpio.23 MISO:gpio.19] [MSG:INFO: SD Card cs_pin:gpio.5 detect:NO_PIN freq:10000000] [MSG:INFO: Stepping:RMT Pulse:4us Dsbl Delay:0us Dir Delay:1us Idle Delay:255ms] [MSG:INFO: Axis count 3] [MSG:INFO: Axis X (150.000,1410.000)] [MSG:INFO: Motor0] [MSG:INFO: tmc_5160 Step:gpio.12 Dir:gpio.14:low CS:gpio.17 Disable:NO_PIN Index:1 R:0.050] [MSG:INFO: X Neg Limit gpio.35] [MSG:INFO: Axis Y (150.000,1402.000)] [MSG:INFO: Motor0] [MSG:INFO: tmc_5160 Step:gpio.27 Dir:gpio.26 CS:NO_PIN Disable:NO_PIN Index:2 R:0.050] [MSG:INFO: Y Neg Limit gpio.34] [MSG:INFO: Motor1] [MSG:INFO: tmc_5160 Step:gpio.33 Dir:gpio.32 CS:NO_PIN Disable:NO_PIN Index:3 R:0.050] [MSG:INFO: Axis Z (-150.000,150.000)] [MSG:INFO: Motor0] [MSG:INFO: tmc_5160 Step:gpio.15 Dir:gpio.2:low CS:NO_PIN Disable:NO_PIN Index:4 R:0.050] [MSG:INFO: Z Neg Limit gpio.39] [MSG:INFO: X Axis driver test passed] [MSG:INFO: Y Axis driver test passed] [MSG:INFO: Y2 Axis driver test passed] [MSG:INFO: Z Axis driver test passed] [MSG:INFO: safety_door_pin gpio.16:low] [MSG:INFO: macro0_pin gpio.13:low] [MSG:INFO: macro1_pin gpio.0:low] [MSG:INFO: Kinematic system: Cartesian] [MSG:INFO: Using spindle NoSpindle] [MSG:INFO: Mist coolant gpio.21] [MSG:INFO: Probe Pin: gpio.22:low] [MSG:INFO: STA SSID is not set] [MSG:INFO: AP SSID FluidNC IP 192.168.0.1 mask 255.255.255.0 channel 1] [MSG:INFO: AP started] [MSG:INFO: WiFi on] [MSG:INFO: Captive Portal Started] [MSG:INFO: HTTP started on port 80] [MSG:INFO: Telnet started on port 23] Grbl 3.7 [FluidNC v3.7.0 (wifi) '$' for help]

$$ $10 = 1 (Status report options, mask) ok $G [GC:G0 G54 G17 G21 G90 G94 M5 M9 T0 F0 S0] ok