Closed bjoerngiesler closed 1 year ago
Works at 100Hz. Still need to check what it does at lower Hz rates to completely understand what's going on here.
Strangely it works at 40Hz too. Huh. Must be a bug I'm doing in the servo code. Closing this ticket.
Right now the absolute rotation values reported by the body IMU are very slow. That is most likely a bug in my usage of the Madgwick filter / IMU updates. This is dependent on the 100Hz initiative, as the IMU spits out data at 104Hz; doesn't make much sense to tackle before that is fixed, but has highest priority directly after, as this is super crucial for smooth control (or even keeping the dome on :-) ).