Closed GoogleCodeExporter closed 8 years ago
The problem was that old (2009) kits shipped with 400 step/rev motors and EBB v
1.1. If EBB v 1.1 is used with newer 200 step/rev motors, then the result is
1600 step/revolution overall.
A workaround was committed for this issue. Create a plain text file named
motor1600.py in the same folder as the eggbot extension. If this file is
present, the software will know that the motors produce 1600 steps per
revolution, and act accordingly.
Original comment by windell@oskay.net
on 31 Aug 2010 at 11:50
Original issue reported on code.google.com by
windell@oskay.net
on 23 Jul 2010 at 9:30