<! -- when I try to raise the drone up it motors just stops working momentary and start working again maybe after the drone is already flipped. it happened to my 3 times and the drone works perfectly fine after the crash and before as well.
Steps to Reproduce
arming the quad
raising the throttle
airmode off
Expected behavior
Additional context
log:
LOG00046.TXT
cli:
INAV_7.1.2_cli_20241106_003329.txt
it shows here in the image throttle is 1000 that can't be for because I have spring centered throttle and I didn't pull it down
Current Behavior
<! -- when I try to raise the drone up it motors just stops working momentary and start working again maybe after the drone is already flipped. it happened to my 3 times and the drone works perfectly fine after the crash and before as well.
Steps to Reproduce
Expected behavior
Additional context
log: LOG00046.TXT cli: INAV_7.1.2_cli_20241106_003329.txt it shows here in the image throttle is 1000 that can't be for because I have spring centered throttle and I didn't pull it down