Hi,
i've downloaded the python render on my linux debian box and plugged the IMU
with a FTDI breakout board.
I've been forced to modify your code and add
line = line.replace("$","") # Delete head "$"
since the program was always reporting "Invalid line".
Now i'm able to see the rendered data but it's a little unstable (little
changes even if left on the table) and above it's wrong:
pitch and roll graphical representation is amplified: 30° real pitch is shown
as 90°, 45° real pitch as about 140-150°
Yaw/magnetic data is almost fixed to East while rotating the board over the yaw
axe, but it's value changes (always with excessive angles) if moving the board
over the roll axe.
Can someone help find out what's happening?
I've started thinking the board is damaged (even if new)...
May the board be running a old fw version (v22) which isn't compatible with
python code?
I wish to see my IMU as in the youtube demo video ;D!
Thanks for your support guys!!
Regards
Gianluca
Original issue reported on code.google.com by gianksm...@gmail.com on 13 Jan 2012 at 3:44
Original issue reported on code.google.com by
gianksm...@gmail.com
on 13 Jan 2012 at 3:44