2nd year electrical engineering team working on a rc car by arduino ,the team is divided into two main groups (Coding team and On ground team) and we are working according to a specified timeline attached in the project ...
After making calculations as explained in wiki(( first circle test page)) we got inaccurate readings it isn't even close to the desired one we faced many problems :
1.wheels are not balanced which affected deviating angle
2.motors where not working as efficient as required so one of them need to be replaced
After making calculations as explained in wiki(( first circle test page)) we got inaccurate readings it isn't even close to the desired one we faced many problems : 1.wheels are not balanced which affected deviating angle 2.motors where not working as efficient as required so one of them need to be replaced