Closed GoogleCodeExporter closed 8 years ago
Logs show the RTL coming home, you cut the radio throttle to zero while it was
in Loiter Mode and entered Stabilize mode with the throttle still cut. So the
model falling out of the sky did exactly as you commanded it.
It's the same as if you were flying manually and pulled the throttle to zero.
It would drop like a rock.
Here is the end of the log: 473(the first field) is your throttle command from
the radio. Time is .1 seconds per entry.
CTUN, 473, 0, 412, 200, 18, 8, -57, 375
CTUN, 473, 0, 403, 200, 21, 9, -74, 379
CTUN, 473, 0, 403, 200, 27, 8, -37, 384
CTUN, 473, 0, 396, 200, 20, 4, -54, 373
CTUN, 473, 0, 387, 200, 23, 3, -72, 375
CTUN, 473, 0, 379, 200, 28, 2, -76, 379
CTUN, 473, 0, 372, 200, 29, 2, -73, 380
CTUN, 473, 0, 356, 200, 30, 4, -117, 383
CTUN, 473, 0, 347, 200, 41, 3, -104, 393
CTUN, 473, 0, 341, 200, 44, 0, -82, 393
CTUN, 460, 0, 336, 200, 38, 2, -66, 389
CTUN, 0, 0, 327, 200, -2, 0, -78, 347 << Throttle input is now zero
CTUN, 0, 0, 327, 200, -19, 5, -39, 335
CTUN, 0, 0, 309, 200, -27, 3, -110, 325
CTUN, 0, 0, 288, 200, -14, 5, -160, 340
CTUN, 0, 0, 263, 200, 0, 5, -205, 354
CTUN, 0, 0, 242, 200, 15, 4, -208, 368
CTUN, 0, 0, 226, 200, 19, 5, -184, 373
CTUN, 0, 0, 228, 200, 14, 7, -82, 370
CTUN, 0, 0, 235, 200, -10, 6, -6, 345
CTUN, 0, 0, 246, 200, -33, 5, 52, 321
CTUN, 0, 0, 251, 200, -52, 5, 51, 302
CTUN, 0, 0, 251, 200, -57, 4, 25, 296
CTUN, 0, 0, 258, 200, -52, 4, 47, 301
CTUN, 0, 0, 260, 200, -57, 1, 33, 293
CTUN, 0, 0, 258, 200, -54, 1, 6, 296
CTUN, 0, 0, 261, 200, -47, 2, 18, 304
CTUN, 0, 0, 261, 200, -49, 2, 9, 302
CTUN, 0, 0, 254, 200, -48, 2, -31, 303
CTUN, 0, 0, 249, 200, -39, 3, -41, 313
CTUN, 0, 0, 247, 200, -34, 4, -31, 319
CTUN, 0, 0, 238, 200, -36, 4, -61, 317
MOD:STABILIZE, 349 << Entering manual control
,3_in, sonar_alt, baro_alt, next_alt, nav_throttle, angle_boost, climb_rate, 3_out, alt_hold_I, throttle_I
CTUN, 0, 0, 233, 200, 0, 1, -56, 0
CTUN, 0, 0, 242, 200, 0, 0, 17, 0
CTUN, 0, 0, 249, 200, 0, 0, 43, 0
CTUN, 0, 0, 247, 200, 0, 0, 11, 0
...Crash...
Original comment by jasonshort
on 22 Oct 2012 at 4:48
but i have not moved sticks, do not change modes and etc. All actions was
automatically after RTL.
when copter fall,- only at this moment i tried to increase the motors speed,
but.. they are not spin, only after crash tried to spin, lol.
Original comment by smscentras
on 22 Oct 2012 at 5:04
So you're saying you didn't enter Stabilize mode and the throttle was at the
mid-point?
You must have lost radio contact then?
Many radios have failsafe defaults that set the throttle to Zero and it could
have also set the CH5 to low or stabilize.
Original comment by jasonshort
on 22 Oct 2012 at 5:15
did not lost radio contact, FrSky with telemetry module do not beep at this
moment.
checked radio failsafe:
throttle: ~45%
mode: RTL
who know where can be problem ?
Original comment by smscentras
on 22 Oct 2012 at 5:39
Maybe this checkbox make problem with throttle ?
Original comment by smscentras
on 22 Oct 2012 at 5:51
Attachments:
Original issue reported on code.google.com by
smscentras
on 22 Oct 2012 at 2:00