Open GoogleCodeExporter opened 9 years ago
They have been tested. The CMDoverwatch will be much stronger than Prototype 2
and will be fully constructed by Thursday Morning. I also noticed a range
issue when using the Robot this morning. The range is about 20m (if that) but
can and should increase with the addition of the High-Power Wireless LAN
adapter that we should get from Mr. S later (hopeful on Wednesday afternoon).
The USB tether should also disappear after Wednesday afternoon as well.
Motors are very powerful, despite the accident that occurred @ 8:27am today.
Original comment by cian.by...@sydstu.catholic.edu.au
on 19 Nov 2012 at 10:51
Motors worked well in prelim testing.
Issues:
- motors came lose from mounts
- massive wheels came off
- the screws holding the axil on disappeared
- massive wheels cause more amps required...only lantern batteries work with
motors now.
Progress on Issues:
- Lose motors:
I have used threadlok on the motors (a glue that goes onto a screw and then
locks the thread in place. I have not checked if this has worked but did
discover in the process that ALL the threads have gone on ALL OF THE MOTORS!
The internal screw hole on the motors have been destroyed (how odd?).
- Wheels coming off / axil screws:
No Progress has been made because I need to buy more Screws which are 1/8th
Inch long. The width is still to be discovered.
- More amps for movement:
Solved: Batteries are semi-permanently attached.
Original comment by cian.by...@sydstu.catholic.edu.au
on 6 Dec 2012 at 10:55
Progress Update:
Wheels are now staying on. This is that's to me working out that the screw
type is a 4 40. I had some leftover from other activities. I drilled them in
and now they won't come off.
Lose motors: The motors are still a bit lose. I will look into this on a
later date. The threadlok might not have worked due to a 4 40 screww being
used instead of a M3 screw. I will see what I can do to resolve this.
#END
Original comment by cian.by...@sydstu.catholic.edu.au
on 21 Dec 2012 at 12:24
New faster motors might be used on CMDRobot (Yet to be named)
Original comment by cian.by...@sydstu.catholic.edu.au
on 13 Feb 2013 at 10:56
motors are stable (except the ones that broke) ;(
Original comment by cmdenterpriseshq
on 2 Apr 2013 at 11:15
Ok sweet, we will update this issue when the ones that have arrived are tested!
Original comment by thomas.i...@sydstu.catholic.edu.au
on 4 Apr 2013 at 2:48
Original issue reported on code.google.com by
cian.by...@sydstu.catholic.edu.au
on 19 Nov 2012 at 2:52