Open gabrielenava opened 3 weeks ago
in the end, after restarting the robot a few times the arm motor moved and we were able to perform our tests. I think the problem is then not the motor, but most likely the 2foc board or some cable that is damaged and might stop working from time to time.
Would it be possible to open the arm and check the cables and board anyways? The robot is now in AMI area
Robot Name 🤖
iCubGenova09 (iRonCub3) S/N:000
Request/Failure description
the right shoulder yaw motor is not moving when a rotation is commanded. After some time, it goes in hardware fault with
i2t limit reached
error. No other messages are provided.Detailed context
We checked the encoder readings and look correct. The problem seems to be related to the motor which is not moving at all.
cc @DanielePucci
Additional context
No response
How does it affect you?
No response