Open S-Dafarra opened 1 week ago
As so far as I remember the problem was due to a missing termination on the CAN. as you can see from the log lines the FW could not add any CAN message, therefore this means that the transmission queue is full, so it seems that the CAN BUS is not operative and the problem is not strictly related to the battery pack since on the same bus there is also the FT sensor.
@MSECode / @AntonioConsilvio / @AntonioAzocar could you please tell me if I'm remembering well?
thanks
Robot Name 🤖
ergoCub 1.3 S/N:002
Request/Failure description
During IROS we noticed the following errors:
Detailed context
The robot was still functional, but this might indicate an issue on the CAN termination. Unfortunately, we don't have the full log.
cc @valegagge @MSECode as we noticed this during IROS
Additional context
No response
How does it affect you?
No response