Closed GoogleCodeExporter closed 8 years ago
After another calibration Yaw (deg) went up to 311.33
Original comment by fouriebrad@gmail.com
on 20 Jan 2013 at 10:30
After another calibration I did a low hover test. The Quad moves to the right
rear as soon as it leaves the ground
Original comment by fouriebrad@gmail.com
on 20 Jan 2013 at 2:09
Hello
Anyone with insight, advice or knowledge on the issue please? Any feedback will
be appreciated.
Thank you
Original comment by fouriebrad@gmail.com
on 26 Jan 2013 at 10:45
Closing all issues on the old issues list by marking them WontFix.
If this is still a valid issue please re-raise it on the new GitHub issues
list: https://github.com/diydrones/ardupilot/issues
Thanks!
Original comment by rmackay...@gmail.com
on 21 Jul 2013 at 2:14
Original issue reported on code.google.com by
fouriebrad@gmail.com
on 20 Jan 2013 at 9:56