The RTC on my prototype is drifting by a couple minutes each day. We need to figure out how to trim it, and the proper way to calibrate that trim in a reasonable time.
Update: I had mistakenly sourced the RTC from DCO instead of XT1, as fixed in 5010755. Reopen the issue if it seems that trimming is in fact necessary.
The RTC on my prototype is drifting by a couple minutes each day. We need to figure out how to trim it, and the proper way to calibrate that trim in a reasonable time.