-
```
What steps will reproduce the problem?
1. Connect with python graphical interface, allow IMU to warm up / initialize
2. Yaw IMU ~90 deg
3. Observe ~44 deg heading change on screen
4. Yaw IMU ~90 d…
-
Can i use this for ros-kinetic?
-
### Description of defect
The orientation sensor on Nicla Sense ME board output bad values.
#### Target(s) affected by this defect ?
Nicla Sense ME
#### Toolchain(s) (name and version) dis…
xamix updated
2 years ago
-
Is there any plan to make more example code for Python just like the Arduino version?
-
-
I have the SparkFun IMU M0, and when trying to upload the sketch, I get the following error:
```
Sketch uses 30,492 bytes (106%) of program storage space. Maximum is 28,672 bytes.
Global variable…
MTDzi updated
6 years ago
-
```
What steps will reproduce the problem?
1. i did not touch the board, try to print the raw data of gyroscope x,y and z
axis.
What is the expected output? What do you see instead?
the z axis valu…
-
Hello,
I am running the python program for the MPU-9250.. Below is the output, but how do I calibrate the MPU ? Please provide exact code for this. I do not have the FaBo9Axis-MPU9250, but just the M…
-
```
What steps will reproduce the problem?
1. i did not touch the board, try to print the raw data of gyroscope x,y and z
axis.
What is the expected output? What do you see instead?
the z axis valu…
-
Hi, is there any way to reduce the noise of the IMU Sensors in the Simulation?
The data below was recorded during a straight acceleration, and as you can see, the noise is quite high (~80% of scale) …